It looks like hell all summer because cattails, hardtack bushes, alders, nightshade and every other sort of pestilential weed grows in it like...well...weeds. 6-8 feet tall.
I used to whack it back with a string trimmer but that's too much like work these days.
Happened to stop by a church rummage sale and found this:


It's a Jari "Chief" sicklebar mower, powered by a nice little (ooooollllddddd....) 3 horse Briggs and Stratton. It was advertised as "only needing the starter fixed". Uh-huh. Well, I fixed the starter and took the completely disintegrated foam air filter off it and re-attached the drive pulley and fired it up. Ran good, cut good for about 10 seconds until the pulley fell off the drive shaft.
Got to looking and the keyway in the drive shaft was all hogged out and the key wouldn't stay in.
Now I'm down to three choices:
1. Weld the pulley on. Dang sure won't come off, but if I NEED to take it off to service a bearing or whatever, I'm screwed.
2. Take the shaft to a machine shop and wait who-knows-how-long for them to weld it up and cut a new keyway in the shaft.
3. Try to cut a new keyway myself.
Of course you KNOW which option I went with. I don't have a Bridgeport, but I DO have a new cross-feed table for my drill press.

I ordered an appropriately-sized cutter from Amazon, set the belt drive for the highest speed, clamped the shaft in the vise that I mounted to my cross-feed table and set the drill press table height to center the cutter on the shaft. (By eye...)

Several very light and well-oiled cuts later, voila! A new keyway. Perfect? Not even close. Good enough for the girls I go with? Absolutely.
I welded up the old hogged-out keyway and started grinding things back to some semblance of roundness. I got it close enough and got the shaft back in the mower and the pulley on, and the pulley stays on and it mows nicely.
However, the bore of the pulley is hogged out as well, and I have no way to to get the shaft truly round, so I think I'll stick a crowbar in my wallet and order up a new shaft and pulley from Jari. But for now, this works.
Couple of notes:
1. I need to take the time to chase out all the threads on the t-nuts on my Grizzly (Chinese) clamp set and get all four corners of the cross feed table clamped down.
2. I need to play with the gib adjustments on the cross-feed and snug it up a bit.
3. Next time I'll move the vise to the right on the cross-feed so the weight is more centered over the drill press table.
All of the above will tighten up tolerances and make for a better job next time.